with Purchase of Furnace & Air Conditioner
Cannot be combined with any other offers. Must present coupon at time of service. Not valid on previously completed work.
To get assistance with your HVAC and plumbing repairs, maintenance, and installations, look no further! To see what our satisfied customers think about our HVAC and plumber services in Prescott, WI, read our reviews below.
Responded to a leaking exterior hose bibb that was losing approximately one gallon of water per day, requiring the homeowner to shut off water nightly to prevent excessive water waste. Upon inspection, confirmed the hose bibb was actively leaking and could not maintain a proper seal. Removed the failed hose bibb and installed a new replacement unit, restoring proper function and eliminating the water loss.
Completed comprehensive HVAC maintenance agreement including furnace and air conditioning system tune-up. Performed furnace operational testing, verified gas pressure settings within specifications, and confirmed temperature rise within acceptable range. Cleaned flame sensor, tested hot surface igniter functionality, and inspected air filter condition. Examined blower compartment and verified proper operation of all components. Switched to cooling mode and measured temperature drop across evaporator coil. Cleared condensate drain lines on both indoor and outdoor units. Performed exterior condenser coil cleaning to remove accumulated debris and ensure optimal heat transfer. Inspected electrical connections, wiring, and components at outdoor unit. All systems tested and operating within manufacturer specifications with no deficiencies noted.
Performed comprehensive operational inspection of natural gas tanked water heater and water softener system in residential basement utility area. Verified proper function of all water heater components including burner assembly, venting system, temperature controls, and pressure relief valve. Checked water softener operation and confirmed adequate system performance. Provided detailed estimate for replacement of existing unit with 50-gallon standard vent natural gas water heater, including specifications for proper venting requirements and installation parameters. Documented existing equipment configuration with copper supply lines, control panel functionality, and current installation setup. All systems found operational at time of inspection.
Completed installation of a 50-gallon power vent water heater in the utility room. Connected all copper supply lines with proper fittings and valves, installed power vent exhaust system with PVC piping, and secured unit to manufacturer specifications. All plumbing connections were tested and verified leak-free, electrical connections completed, and system is fully operational.
Responded to no heat call on furnace over 10 years old with flashing ignition failure code on control board. Diagnosed failed gas valve preventing fuel delivery to burner assembly despite pilot ignition attempts. Replaced defective gas valve and restored heating operation. Comfort advisor consulted regarding system age and long-term options.
Responded to service call for whistling toilet and dishwasher drainage issues. Completed full replacement of two existing toilets with new Toto comfort height elongated ADA-compliant models. Removed old fixtures, installed new toilets with proper sealing and water supply connections, and tested both units for proper operation and leak-free performance.
Completed annual AC tune-up and maintenance on Bryant air conditioning system. Performed comprehensive inspection including temperature split verification, filter examination, electrical connection testing, and adjusted humidifier settings to summer mode. System operating within normal parameters with no issues identified during service visit.
Removed existing dryer vent system and installed new dryer venting from the appliance location through the building structure to the exterior termination point. The installation required routing the metallic ductwork through unfinished interior spaces and securing it properly with metal straps to ensure code-compliant clearances and proper support. Work was completed by a two-person crew over a three-hour period.
Responded to gas line damage caused by excavator strike. Upon inspection, found copper gas line kinked in two locations—at the meter connection and where the line enters the house. Attempted to pull the damaged section to perform a splice repair, but the line was solidly embedded in the wall and could not be extracted without causing further damage. Due to the finished basement preventing interior wall access and the extent of the damage at both the meter and building entry points, determined that a complete line replacement from the gas meter to the mechanical room would be required. Documented the damage with photographs showing the kinked piping at the meter assembly and the exterior penetration point. Coordinated with advisor to schedule a site visit for bidding the full line replacement work.
Responded to no heat and no hot water complaint on residential boiler system installed in 2020. Upon arrival, found boiler not firing and multiple water leaks present in the system. Diagnosed leaking shut-off valve on auto-fill system; isolated valve to stop active leak. Identified leaking ball valve at circulator pump, tightened compression nut to eliminate leak. Auto-fill system found to be non-functional, preventing proper system pressurization. Manually added water to boiler to restore proper operating pressure. Successfully started system and verified boiler ignition and proper operation of all components. Located additional leak at fitting above water heater requiring specialized part not currently in stock. System restored to full operation with temporary repairs holding. Provided estimates for permanent repairs including replacement of auto-fill shut-off valve and auto-fill assembly to prevent recurrence. Parts order submitted for water heater fitting repair. System operational
Completed routine plumbing inspection of mechanical space focusing on insulated piping systems. Documented condition of foam-insulated pipes, verifying proper insulation coverage and integrity of HVAC/plumbing components. All insulated piping found to be in standard working condition with no visible damage or deterioration requiring immediate attention.
# Warranty Service Report Completed warranty service call for furnace control board replacement. Installed new control board under warranty coverage and attempted system startup. Upon initial testing, furnace exhibited same failure symptoms as original service request. Performed diagnostic troubleshooting of all associated components and discovered low pressure (LP) switch sensor connection was not fully seated. Reconnected LP sensor to proper specification, ensuring secure connection. Conducted full system startup sequence and verified furnace ignition and operation within normal parameters. Unit now cycling and heating properly. Advised customer to contact for service if any further issues arise.
# Service Report: No Heat - Furnace Control Board Failure ## Summary Responded to no-heat callback on residential furnace following resolution of basement flooding issue. Diagnosed failed control board not providing 24-volt signal to gas valve and completed warranty replacement to restore heating operation. ## Service Details Arrived on-site for follow-up service call after customer reported furnace remained non-operational. Previous day's service was postponed due to flooded basement conditions caused by backed-up sewer line, which had since been remediated by separate contractor. **Diagnostic Findings:** - Conducted systematic electrical diagnostics on furnace control system - Verified proper incoming power supply to unit - Tested thermostat call for heat signal - functioning correctly - Measured output voltage from control board to gas valve - Confirmed control board failure - no 24-volt output signal present at gas valve terminals - Gas valve itself tested within normal operati
Responded to no heat call for furnace installed last year. Discovered significant basement flooding with sewage backup that compromised the system drain line. Vacuum-cleaned the drain line to restore proper drainage functionality and tested system operation after addressing the water damage.
Disconnected electrical circuit from jetted tub as part of conversion to shower installation. Properly terminated wires in junction box and turned off breaker while maintaining circuit integrity for potential future use. Verified water heater and associated plumbing connections in utility room were in normal working condition with no visible issues.
Responded to service call for Alpine 600 humidifier leaking water onto floor. Cleaned water line hose and restored proper operation. Observed significant calcium buildup on recently replaced humidifier pad, indicating potential water softener malfunction. Scheduled water quality analysis to address recurring mineral accumulation issues.
Installed new mop sink faucet in utility area after diagnosing missing main ball valve handle. Added necessary valve after the meter and completed plumbing connections by transitioning from existing metal pipe to PEX line, ensuring proper water supply to the fixture.
Responded to no-heat call on propane furnace installed last fall. Diagnosed E270 soft lockout condition caused by leaves obstructing combustion air intake on burner grill. Removed debris, reconfigured staging jumpers to properly enter second stage after 12 minutes (system previously failed to reach second stage after 20+ minutes of operation), and verified proper system operation. Noted significant ductwork issues causing excessive noise during operation and observed improper termination requiring remediation.
Responded to a service call for a 2022 electric tanked water heater that was not producing hot water after the residence had been vacant for approximately one month. Diagnostic testing identified a faulty bottom heating element as the source of the problem. Replaced the bottom element, restoring proper functionality to the unit.
Performed free furnace tune-up on 3-year-old unit, confirming all components operate within specifications. Adjusted gas pressure to proper range, verified safe CO levels in flue, and identified dirty blower wheel requiring cleaning. Recommended future blower wheel service to maintain optimal system performance.
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