with Purchase of Furnace & Air Conditioner
Cannot be combined with any other offers. Must present coupon at time of service. Not valid on previously completed work.
Responded to kitchen plumbing issues involving water leak beneath sink and slow drainage. Removed and replaced deteriorated kitchen faucet with new Moen unit to eliminate leak source. Addressed drainage problem by running mechanical drain snake through kitchen sink drain line to clear blockage and restore proper flow. All plumbing connections tested and verified leak-free upon completion.
Responded to no heat call on 1994 Lennox propane furnace. Upon arrival, found pilot would ignite but main burner would not light, with igniter sparking continuously for approximately 30 seconds before system shutdown. Removed pilot assembly and thoroughly cleaned spark rod, flame sensor, and verified pilot tube was clear of obstructions. Reinstalled pilot assembly and tested system operation—unit now igniting properly and heating as designed. Performed visual inspection of heat exchanger with no condemnable cracks observed.
Installed customer-supplied Moen tub and shower valve assembly at the residence. Arrived on-site during the scheduled window, contacted customer prior to arrival as requested, and successfully completed the installation of the new valve system.
Responded to water leak emergency in basement originating from shower area. Upon arrival, water supply to home was shut off due to broken Delta valve in wall, damaged during attempted self-repair. Installed temporary shut-off valves to restore water service to remainder of home while isolating the compromised shower fixture. Follow-up appointment scheduled pending estimate approval for complete valve replacement and permanent repair.
Responded to emergency call for leaking 50-gallon electric water heater with water discharge from bottom of tank. Upon arrival, shut off water supply and drained the unit to prevent further water damage. Inspection confirmed failed tank integrity requiring full replacement. Removed existing failed water heater and installed new 50-gallon electric Bradford White water heater, reconnected all electrical and plumbing connections, and tested unit for proper operation.
Responded to water leak complaint under kitchen sink at residential property. Upon inspection, identified garbage disposal as source of leak. Removed failed garbage disposal unit and installed new sink basket strainer assembly in double-basin stainless steel sink. Verified all drain connections were properly sealed and tested system for leaks. No further water intrusion detected upon completion.
Performed inspection of residential plumbing system to verify pipe sizing, confirming 1-1/2" L copper piping installation. Documented existing HVAC and plumbing configuration including ball valve connections, PVC supply lines, and mechanical equipment layout. Provided consultation regarding electronic anode rod installation options for water heater system.
Replaced exterior hose bibb that was plumbed through crawl space, installing new frost-free spigot in recessed wall box with proper mounting to exterior siding. Rebuilt second hose bibb located at kitchen side of home, replacing worn valve assembly and ensuring proper shutoff function. Replaced hose bibb under kitchen sink, integrating new valve with existing water filtration system and supply lines while maintaining proper connections to copper supply pipes and PVC drain assembly.
Completed annual air conditioning tuneup and preventative maintenance inspection per service agreement. Performed comprehensive system evaluation including visual inspection of air handler, motor assembly, ductwork, and electrical connections. All components found operating within normal parameters with no deficiencies noted. Refrigerant charge assessment deferred due to ambient temperature conditions being too low for accurate readings; system not requiring refrigerant service at this time. Unit confirmed operational and ready for cooling season.
Completed annual cross-control backflow prevention inspection and testing on two devices: a Wilkins 975XL RPZ valve (serial number ABB08849) located in Washroom #2 and a Wilkins 460XL SVB valve (serial number 461483) located at the freezer wall. Both assemblies passed testing with acceptable differential pressure readings recorded for check valves and relief valve components. Additionally, replaced a malfunctioning foot-activated mixing valve at the hand wash sink to restore proper operation.
Responded to commercial customer complaint of low water pressure affecting dishwasher operation. Diagnosed faulty solenoid valve as the root cause of insufficient water flow. Ordered replacement cleanout cover to address broken component and submitted part order form per management instruction.
Installed new single compartment sink and wall mount sink with faucet in janitor's closet area. Ran water lines overhead with insulated PEX piping and connected drain to open site adjacent to sink. Capped existing shutoff (CR19) with PEX plugs as requested.
Conducted comprehensive inspection of toilet reported for leaking issues. Identified significant mineral buildup and aging components within the tank, including worn flush valve and deteriorated flapper mechanism. Provided on-site assessment and repair options to resolve the water leakage problem.
Responded to no-heat call for newly installed furnace. Diagnosed shorted limit switch as the source of the heating failure and non-functional thermostat. Implemented temporary repair to restore heat safely until permanent replacement can be performed.
Replaced 17-year-old 40-gallon LP water heater due to pressure switch failure resulting in no hot water. Installed new Bradford White water heater with proper connections to existing plumbing and gas lines, ensuring proper insulation of copper pipes.
Successfully diagnosed and replaced faulty control board on Richmond furnace. Upon installation of new control board (part #215172-001), tested system operation with positive results. Unit is now heating properly with all functions restored to normal operation.
Responded to no heat complaint on 10+ year old ICP high efficiency furnace. Diagnosed high limit switch tripped due to plugged filter. Reset high limit switch, replaced filter, tested furnace operation, and installed new high limit switch to restore proper heating function.
Responded to call regarding frozen furnace vent pipe. Upon arrival, customer had already cleared ice blockage and furnace was operational. Identified improper venting configuration with approximately 30 ft run under deck causing condensation freezing issues. Consulted with Jordan who scheduled follow-up visit to evaluate alternative venting locations to prevent future freezing incidents.
Responded to no-heat call for Lennox pulse furnace in lockout condition. Diagnosed failed control board and performed pressure test on heat exchanger, which revealed significant leakage. Due to safety concerns, tagged and locked out furnace. Customer is temporarily utilizing electric backup heating while awaiting quote for furnace replacement.
Responded to no-heat call for an 8-year-old furnace exhibiting pressure switch code failure. Diagnosed intermittent power loss to inducer motor despite call for heat at W terminal. Located faulty connection at control board and identified heat exchanger joint leak. Recommended control board replacement and blower wheel cleaning due to significant dirt accumulation affecting system performance.
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