with Purchase of Furnace & AC
Includes Merv 16 5" media cabinent and ApcoX Premium UV-light. Cannot be combined with any other offers. Must present coupon at time of service. Not valid on previously completed work.
When you have your furnace or plumbing systems repaired or installed by Hurlburt, you can be assured that it is done right. To read about other customers’ experiences with our furnace and plumber services in Knapp, WI, check out our online reviews below!
Responded to no cool call on an 8-year-old residential air conditioning system using R22 refrigerant. Upon arrival, verified system was achieving a 14-15 degree temperature split but unable to maintain desired setpoint. Diagnosed system as low on refrigerant charge, indicating a leak in the system. Advised customer that while recharging is possible, system replacement is recommended due to age, refrigerant type, and recurring refrigerant loss. Customer declined service at this time and will contact for replacement estimate at a later date.
Replaced failed expansion valve (TXV) and RDS control board on Goodman HVAC system. Installed new components, performed verification test to activate RDS settings on integrated furnace control, and adjusted blower speed to match 2-ton system capacity. Evacuated refrigerant lines, recharged system with R32 refrigerant, and conducted operational testing. System now operating within specifications with proper temperature split across furnace.
Completed comprehensive AC tune-up on Lennox condensing unit as part of maintenance agreement. Replaced indoor air filter, verified evaporator drain line proper operation, removed condenser panels and thoroughly cleaned condenser coil which showed significant buildup from four years without service. Inspected electrical components including capacitor (within specification) and contactor (good condition). Addressed homeowner concern regarding unusual noise during unit shutdown, identified as refrigerant flow noise due to dirty condenser coil restricting airflow. System startup confirmed proper operation with 22-degree temperature split across evaporator coil, indicating adequate cooling performance and refrigerant charge.
Responded to no cooling complaint on 10+ year old R22 system that had been recently serviced by another contractor. Upon inspection, determined the thermostatic expansion valve (TXV) requires replacement, likely due to improper installation procedures including failure to flow nitrogen during brazing operations. System also requires installation of RDS mitigation board for code compliance. Documented equipment condition with photos and requested pricing for TXV replacement and required safety component installation to restore proper system operation.
Responded to no-cool call on 2008 Ruud outdoor condensing unit. Upon arrival, unit was attempting to start but failing to run, with audible clicking from contactor and loud buzzing noise. Diagnosed failed capacitor with no measurable capacitance and severely pitted contactor causing poor electrical contact. Replaced both capacitor and contactor with OEM-equivalent parts. Rinsed outdoor coil to remove debris accumulation. Verified proper system startup with 18-degree temperature split across evaporator coil, confirming adequate cooling performance restored.
Performed comprehensive AC tune-up on Lennox system for homeowners who recently moved into the property and were starting the unit for the first time. Upon inspection, discovered system was significantly low on refrigerant charge. Discussed diagnostic findings and repair options with homeowner, who authorized addition of refrigerant and UV dye to restore system operation. Added refrigerant to manufacturer specifications, achieving proper operating pressures with 20° temperature split and 3° subcool. Injected UV dye into system for future leak detection purposes. System now operational and cooling effectively.
Responded to no cooling complaint on one-year-old Goodman system running continuously. Inspected indoor coil and confirmed no freeze-up, though evidence of water on floor indicated previous freezing condition. Connected manifold gauges and found near-zero suction pressure and low liquid line pressure. Identified active refrigerant leak at outdoor unit Schrader valve, documented with video evidence. Performed bubble test on all accessible refrigerant connections with no additional leaks detected. System confirmed low on R32 refrigerant. Scheduled follow-up visit to replace leaking Schrader valve and recharge system with R32 refrigerant once pricing and materials are obtained.
Responded to a dual plumbing issue involving a leaking Delta shower valve and a clogged kitchen sink drain. Upon inspection, found the shower valve cartridge was failing and causing water to leak from the handle. Replaced the Delta cartridge to restore proper function and eliminate the leak. For the kitchen sink, diagnosed a grease blockage in the horizontal drain section before the vertical drop. The homeowner had previously attempted to clear the obstruction and noted a gel-like substance in the pipes. Used a drain auger to break up the grease accumulation, then employed a blow bag to fully clear the line and restore proper drainage. The blockage was successfully removed from the accessible horizontal pipe section without requiring extensive disassembly of the drain system.
Performed comprehensive evaluation of residential heating system for new homeowner unfamiliar with boiler operation. Inspected HeatMaster GS200 Titanium outdoor wood-burning furnace located in open-sided shelter structure. Unit displayed significant paint deterioration and surface wear on upper sections, exposing underlying metal substrate. Discovered critical freeze damage to outdoor furnace cabinet, with housing compromised and broken open due to freezing conditions. Assessed indoor mechanical room containing hydronic heating distribution system with multi-zone manifold assembly, including multiple zone valves with blue handles, pressure gauges, and copper piping network. Evaluated green circulation pump control system and associated plumbing connections. Documented existing system configuration including reflective insulation installation, PVC and copper piping arrangements, and manifold pressure monitoring equipment. Coordinated with sales department to schedule estimate for replac
Diagnosed furnace short cycling issue caused by inadequate airflow. Identified improper transition size restricting airflow and causing limit switch activation. Sealed gap behind thermostat to prevent cold air infiltration affecting temperature readings. Will return with correct size transition and new limit switches to improve system performance.
Responded to service call for kitchen sink backup and leak under sink when laundry was in use. Diagnosed cross-connection between kitchen and laundry drain systems causing simultaneous backups. Snaked kitchen drain line to clear obstruction and inspected laundry drain configuration, confirming proper venting and drainage pathway to prevent future backups.
Responded to service call for in-floor heating system with reported leak filling bucket every two days. Upon inspection, identified backflow preventer as source of leak, successfully repaired the issue, and completed documentation for potential replacement if needed in future. System appears to be in good working order with no further leaks observed.
Inspected and serviced bathroom exhaust fan that was leaking water. Upon investigation, determined the source of the leak was a damaged roof jack, not the fan unit itself. Disassembled fan assembly, performed thorough cleaning, and verified proper operation. Homeowner has scheduled a roofing contractor to repair the compromised roof section.
Responded to service call regarding dishwasher drainage issues. Inspection revealed 20+ year old unit with failing drain pump. Checked plumbing connections including PVC drain lines and air core ventilation pipes; all connections secure with temporary tape seals observed at pipe junctions. Advised customer that replacement of dishwasher unit is recommended rather than repair due to age of appliance.
Responded to customer complaint of sewage odor in kitchen drain. Diagnosed improper dishwasher drain installation with no high loop and excessive insertion into standpipe. Corrected by installing proper high loop and reducing insertion depth to 5-6 inches, eliminating sewer gas backflow risk.
Completed warranty repair involving replacement of control board due to intermittent furnace operation. Removed undersized damper beneath furnace to improve airflow, as the existing setup featured very restricted ductwork openings. Advised customer that rapid temperature fluctuations are likely due to insulation characteristics of manufactured home and small ductwork configuration, which cannot be easily modified.
Installed new high limit switch on furnace after diagnosing a tripped limit/roll-out issue. Reset safety controls, performed comprehensive operational testing, and verified system functioning correctly.
Responded to furnace short cycling complaint. Found inducer filled with water due to improper coupling angle causing air lock before drainage. Repositioned inducer coupling downward and adjusted vinyl tubing connection to improve drainage. Additionally diagnosed erratic thermostat behavior at setpoint; replaced thermostat which resolved irregular cycling issues. System now properly maintaining temperature and shutting off appropriately at setpoint.
Performed standard furnace maintenance tune-up on residential unit. System functioning within normal parameters after cleaning flame sensor, testing electrical components, and removing wasp nest from intake. No operational issues detected.
Diagnosed furnace's no-heat condition caused by faulty limit switch with damaged internal contacts (snap disc style). Verified filter was clean and installed temporary replacement limit switch to restore heat operation. Permanent replacement part has been ordered and will be installed on follow-up service call.
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