with Purchase of Furnace & Air Conditioner
Cannot be combined with any other offers. Must present coupon at time of service. Not valid on previously completed work.
Responded to no heat call for 3-year-old Lennox system displaying "GS calibration failure 276-692" error. Diagnosed concentric venting issue with blocked exhaust side. Temporarily rerouted exhaust vent through the incoming vent and utilized basement air for combustion to restore heat function. Proper venting configuration will require permanent repair.
Repaired the furnace by replacing damaged burners and repairing the flared connection on the copper gas line. Verified no gas leaks after repair and confirmed unit ignition. Unit tripped rollout switch due to excessive soot accumulation in heat exchanger from previous burner damage; recommended heat exchanger or complete furnace replacement.
Responded to no-heat call and diagnosed multiple issues with furnace. Found burners with significant rollback, removed and inspected to discover two cracked burners and a gas leak at deteriorated copper flare connection. Replaced damaged burners and performed repair by cutting and re-flaring gas line to restore safe operation.
Responded to emergency service call for sole household toilet clogged with blockage approximately 5 feet down waste line. Initial plunging attempts unsuccessful; successfully cleared obstruction using toilet auger. Additionally addressed secondary issue of shower backup, which required drain clearing procedures to restore proper drainage function in both fixtures.
Replaced leaking 40-gallon LP water heater that showed significant corrosion at connection points. Installed new A.O. Smith ProLine XL commercial series water heater with proper copper piping and fittings, resolving the water leakage issue.
Diagnosed inoperative oil furnace finding multiple critical defects: burner cone completely broken, improperly adjusted electrodes, and incorrect nozzle installation (evidenced by significant internal sooting). After assessment, determined extensive repairs would likely cause additional component failure. Recommended complete furnace replacement as the most practical solution, which customer approved. Scheduled follow-up appointment to review new furnace options.
Responded to health inspector compliance issue by installing an air gap on food prep sink that was previously connected incorrectly. Attempted to address two urinals with slow drainage but determined they required professional drain cleaning. Referred client to Roto Rooter for urinal service as the blockage was beyond standard maintenance capabilities.
Performed annual furnace tune-up on 2-year-old FRP heat pump system. Replaced dirty humidifier pad and filter. Inspected all components including blower (clean and balanced), electrical components (within spec), condensate lines (clear), and heat exchanger (no compromises). System operated normally during 15-minute test run with 60-degree temperature rise. Reviewed whole home dehumidifier operation with customer per their request.
Performed routine furnace tune-up on 8-year-old FRP unit. Inspected components including filter (noted as requiring replacement), blower (clean and balanced), and heat exchanger (no compromises). Identified leaking inducer seal at collector box causing noise and potential electrical hazard. Tested system operation for 20 minutes with proper gas pressures and verified venting integrity. Customer requested estimate for inducer motor repair.
Performed furnace tune-up on a 17-year-old natural gas regulator that was improperly installed for an LP gas single-stage furnace serving three zones. Inspected the heat exchanger and condenser coils, noting debris accumulation requiring cleaning. Examined the Honeywell digital thermostat which was functioning properly with correct temperature readings. Customer indicated limited interest in full system replacement at this time.
Completed duct cleaning service as part of installation package. Inspected and cleaned ductwork connected to wall-mounted air vents, ensuring proper airflow and system efficiency. Verified installation integrity of rectangular metal vent access points throughout the home.
Performed comprehensive duct cleaning service in conjunction with new HVAC system installation. Cleaned and inspected all accessible supply and return air vents throughout the property, ensuring proper airflow and system efficiency.
Completed annual HVAC maintenance on 19-year-old gas furnace for new customer. Inspected heat exchanger which appeared in acceptable condition despite age, with evidence of previous repairs. Noted adjacent 80-gallon water heater with visible leak dripping onto floor from pedestal. Customer scheduled follow-up appointments for equipment replacement quotes for both HVAC and plumbing systems.
Performed scheduled maintenance on geothermal system including temperature readings, pressure verification, and component inspection with all systems functioning properly. Conducted thorough inspection of G32 gas furnace including heat exchanger examination, flame sensor and condensate cleaning, with no defects identified. Serviced steam humidifier which exhibited frequent flushing cycles due to ongoing water conductivity issues, and performed maintenance on separate oil furnace including nozzle and filter replacement.
Responded to no-heat complaint on dual electric/oil furnace system. Diagnosed failed electric plenum heater with burnt contactors and 24V coils as confirmed by visual inspection. Customer has been relying on oil furnace for heat. After discussing repair options, customer elected to discontinue electric heating repairs in favor of converting to LP due to high utility costs from electric heat usage. Scheduled advisor visit for LP conversion consultation.
Responded to no heat complaint on 5-6 year old LP furnace. Diagnostic testing revealed gas valve was not energizing despite receiving 26 volts. Replaced gas valve under warranty coverage and verified proper system operation with successful heat production.
Responded to service call for handicap toilet in men's restroom that was overflowing. Diagnostic inspection revealed broken flush valve component. Shut off water supply, disassembled tank, and replaced defective flush valve part. Tested toilet operation after repair to confirm proper function with no further leaking or overflow issues.
Connected commercial stainless steel utility sink to waterline in utility room. Installed single basin sink with backsplash against wall, ensuring proper water connections. Verified system functionality after installation.
Responded to service call for a clogged urinal. Disassembled the urinal fixture, performed drain snaking procedure to clear the blockage, then reassembled the unit. Verified proper drainage function before completing the service.
Inspected Navien tankless water heater (model NPE2400) exhibiting error codes and found significant corrosion around the recirculation pump and heat exchanger. Recommended tuneup service to address these issues. Also assessed backing up urinal and recommended augering to clear the blockage.
©2026 Hurlburt. All Rights Reserved.
Privacy Policy | Terms and Conditions | [cookie_preferences_link]
This site is protected by reCAPTCHA and the Google Privacy Policy and Google Terms of Service apply.